Our
running
season
officially
ended
on
25th
October,
though
by
special
request,
we
did
host
a
party
in
November.
We
would
not
normally
host
parties
beyond
the
end
of
our
running
season,
not
least
because
the
weather
is
often
less
kind,
but
everything
worked
out
just
fine
on
this
occasion.
Our
next
running
season
is
scheduled
to
begin
on
3rd
April
2016, weather permitting.
We
carried
a
total
of
1709
passengers
at
our
track
site
during
the
year
(excluding
parties)
compared
to
1647
in
the
previous
year
and
1738
the
year
before
that.
So,
a
pleasing
result
I
would
say.
During
the
season
we
also
arranged
15
children’s
parties,
this
compares
to
11
the
previous
year
and
5
in
2013.
I
would
not
like
to
hold
any
more
than
we
did
in
the
current
year
as
we
do
not
have
the
manpower
to
spread
the
workload.
I
am
pleased
to
report
that
all
the
parties
went
off
without
incident
and
I
would
like
to
thank
all
concerned
for
their vigilance.
Towards
the
end
of
the
year
there
were
reports
that
our
petrol
locomotive,
Green
Dragon,
had
lost
some
power.
It
was
having
difficulty
pulling
a
load
up
our
steep
gradient.
Since
we
had
a
children's
party
coming
up,
a
week
later,
we
decided
not
to
try
and
diagnose
the
problem
but
to
change
the
petrol
engine
for
a
new
identical
one
we
had
on
the
shelf.
This
was
done
and
we
have
had
no
power
problems
since
the
change
over,
but
the
engine
has
not
had
extensive
testing
as
the
repair
was
done
only
a
few
days
before
the
seasons
last
run.
Only
when
the
engine
change
was
almost
completed
did
we
notice
that
an
angle
iron
bracket,
that
supported
a
quadrant
which
turned
the
throttle
cable
through
90
degrees,
had
come
loose
and
was
flexing
and
possibly
not
allowing
the
throttle
to
open
fully.
This
is
pure
conjecture
but
a
possibility
none the less.
Whilst
on
the
subject
of
locomotive
problems
we
discovered
that
our
Wren
loco
was
using
a
considerable
amount
of
coal
when
running
in
full
gear,
in
fact
significantly
more
than
drivers
could
remember
it
doing
in
the
past.
When
setting
off
from
our
raised
track
station
with
a
full
load,
a
freshly
charged
fire
would
normally
allow
three
laps
to
be
completed
before
the
fire
needed
refilling.
When
the
problem
reared
its
head
we
had
to
refill
the
fire
before
half
a
lap
had
been
completed.
The
chimney
exhaust
note
was
very
fierce
resulting
in
unburnt,
but
shattered,
coal
being
pulled
off
the
fire.
We
were
able
to
continue
using
the
loco
throughout
the
season
by
running
notched
up,
including
setting
off
notched
up,
and
this
allowed
us
to
fire
at
the
rate
we
were
accustomed
to.
Over
time
the
various
parts
of
the
valve
gear
have
worn
and
the
accumulated
wear
has
resulted,
presumably,
in
excessive
valve
movement,
such
that
steam
is
being
admitted
to
the
cylinder
for
virtually
the
whole
stroke.
At
least
that
is
what
we
think
is
happening
and
we
shall
over
the
next
few
months
remake
and
rebush
the
affected
parts.
Running
notched
up
of
course
brings
the
valve
events
to
something
like what the correct full gear should be if there was no wear.
In
my
previous
report
I
mentioned
that
one
outside
event
was
still
outstanding.
That
event
was
the
Dickensian
themed
event
in
Rotherham
town
centre.
We
like
to
attend
this
event
as
Rotherham
is
our
home
town,
our
portable
track
is
easy
to
set
up,
the
local
authority
personnel
are
very
accommodating
and
it’s
a
good
way
to
advertise
ourselves
to
the
local
community.
All
our
equipment
had
been
loaded
onto
trailers
a
few
days
earlier
and
we
were
good
to
go.
On
the
morning
of
the
event
we
got
word
that
the
event
was
being
cancelled
on
safety
grounds
due
to
severe
gales.
Luckily
we
got
the
news
before
anyone
had
actually
set
off
-
and
if
the
truth
be
known
I
for
one
was
pleased
because
it
was
a
really
wet
and
windy
day.
We
would
not
have
got
any
passengers
in
those
conditions anyway.
Dr.Paul
has
been
rebuilding
his
Wren
for
over
a
year
now
but
finally
the
rebuild
is
complete
and
a
fine
looking
loco
it
is
in
its
new
green
livery
(see
photo).
The
boiler
was
hydraulically
tested
before
it
was
put
back
in
the
frames
and
so
all
that
remains
to
be
done
is
a
steam
test.
I
should
mention
that
Geoff
Symms
and
Les
Davies
have
helped
in
this
rebuild
for
most
of
the
time
it
has
taken.
Geoff
in
particular
overseeing
much of the painting work.
The
seat
covering
of
most
of
our
rolling
stock
is
starting
to
get
a
little
(but
only
a
little)
tatty,
so
over
the
close
season
we
will
replace
it.
Arthur
Hague
has
started
this
job
but
I'm
sure
others
will
join
him
in
the
coming
weeks.
There
are
eight
coaches
involved,
four
ground
level
coaches
and
four
from
the raised track.
We
have
two
new
members
to
welcome,
Ken
Brown
and
Stan
Glover.
I
hope
we
will
see
them
at
the
track
as
often
as
their
personal
circumstances
will
allow.
We
have
already
hydraulically
tested
Ken's
traction
engine
boiler
which
is
of
steel
construction
but
the
noteworthy
aspect
of
this
boiler
is
that
the
firebox
stays
are
of
the
threaded
and
nutted
variety
which many would consider to be outdated.
You
may
recall
that
when
discussing
the
progress
of
our
new
diesel
hydraulic
loco
I
have
in
the
past
mentioned
the
possibility
of
the
loco
running
away
on
the
downhill
gradient
that
is
a
feature
of
our
track.
In
that
regard
I
have
mentioned
that
over
centre
valves
may
need
to
be
fitted
to
ensure
that
this
could
not
happen.
In
tests
it
did
in
fact
prove
to
be
the
case
that
the
loco
would
gain
speed
when
going
downhill
regardless
of
the
position
of
the
control
lever.
A
few
weeks
ago
we
fitted
two
OCV's,
one
on
the
hydraulic
motor
of
each
bogey.
This
was
not
without
its
problems
but
eventually
we
got
them
to
work
and
they
do
the
job
they
are
designed
to
do.
The
loco
can
be
brought
to
a
complete
standstill
by
use
of
the
control
lever
alone
on
the
steepest
downhill
gradient
and
the
loco
can
be
brought
to
a
standstill
on
the
up
gradient
without
it
rolling
backwards
i.e.
with
the
control
lever
in
neutral.
The
only
problem
is
the
maximum
speed
of
the
loco
is
much
reduced
and
the
engine
will
not
rev
when
under
load.
Remember
this
is
a
20hp
(or
there
a
bouts)
engine
compared
to
our
existing
petrol
loco
which
is
6.5hp.
With
the
control
lever
in
neutral,
the
engine
revs
as
designed
to
give
a
flow
rate
of
80
litres/minute
-
the
designed
flow
rate
-
hydraulic
fluid
flows
from
the
pump
through
the
flowmeter
and
via
the
control
block
back
to
tank.
But
as
soon
as
the
control
lever
is
moved
and
hydraulic
fluid
is
being
sent
to
the
motors
the
flow
rate
drops
to
less
than
60
litres/minute
with
the
maximum
speed
being
proportionally
reduced.
At
this
moment
the
solution
is
not
clear
but
we
are
working
with
people
who
have
a
better
understanding
of
these
things
than
we
have
and
with
so
much
effort
having
already
gone
into
the project we will do whatever we have to do.
On
a
brighter
note
the
brake
bands
have
now
been
fitted
to
the
brake
drums
on
the
new
hydraulic
loco
and
the
design
and
outline
of
the
nose
ends
of
the
type
37
diesel
have
been
drawn up with a view to their manufacture in due course.
I
did
say
in
my
last
report
that
if
anyone
wished
to
contribute
to
the
newsletter
on
any
matter
that
members
may
be
interested
in,
the
editor
would
be
pleased
to
include
such
articles in a future edition.
It
only
remains
for
me
to
wish
everyone
a
happy
new
year
and thank members for their support in the past year.
Dennis Meares
Chairman